Created Thursday, Jul 13th 2023 06:24Z, last updated Thursday, Jul 13th 2023 06:24Z
A Fedex Federal Express Boeing 767-300 freighter, registration N146FE performing flight FX-1026 from Newark,NJ to Los Angeles,CA (USA) with 2 crew, was on final approach to Los Angeles's runway 24R when the crew received an unsafe gear indication, the left main gear was not down and locked. The aircraft went around and entered a hold at 5000 feet while the crew was working the checklists. The aircraft subsequently performed a low approach to runway 24L, an inspection from the ground could not solidly determine whether the left main gear was down, the gear doors were open. Tower offered to have somebody placed to the runway for another inspection from the ground, the crew decided to perform another low approach. The aircraft positioned for another approach to runway 24L descending to about 300 feet now. Operations vehicles placed along the runway reported the left main gear did not appear in position. The crew advised they needed to talk to operations and maintenance, but they suspected there was not a lot more they could do. The aircraft entered another hold at 5000 feet for about 40 minutes, then performed a partial gear down landing on runway 25R about 45 minutes after the second low approach. The aircraft came to a stop on the center line of the runway sitting on its nose gear, right main gear and left engine cowling. The crew evacuated the aircraft through the cockpit window via a rope. The first officer received serious injuries during the evacuation.
On Aug 20th 2020 the FAA reported the aircraft landed on one main gear only. One of the pilots received minor injuries, the other remained uninjured.
On Aug 21st 2020 the FAA changed to report, the injury of the one pilot is now rated serious.
On Aug 28th 2020 the NTSB reported the left main gear failed to extend. The aircraft sustained substantial damage, the first officer received serious injuries while exiting the cockpit via the emergency escape rope. The NTSB is investigating.
On Jul 13th 2023 the NTSB released their final report concluding the probable cause of the accident was:
The left main landing gear’s failure to extend due to the separation of the brake rod retaining hardware from the aft inboard wheel for reasons that could not be determined based on the available evidence.
The NTSB analysed:
In preparation for landing, LAX air traffic control cleared FedEx flight 1026 for an instrument landing system (ILS) approach to runway 24R. When the airplane descended to an altitude of about 1,800 ft, the flight crew moved the landing gear handle to lower the landing gear. The crew then received a “GEAR DISAGREE” message from the engine indicating and crew alerting system. The crew discontinued the approach and climbed the airplane to 5,000 ft to perform the quick reference handbook Gear Disagree checklist procedure. The checklist directed the crew to lower the landing gear using the alternate gear extension system, but the left main landing gear (MLG) still did not extend.
The flight crew then flew a low approach to the runway so that the tower controller could try to see if the left MLG was extended. The airplane descended to an altitude of about 500 ft above ground level, but the tower controller could not tell whether the left MLG was extended. The crew then declared an emergency and flew another low approach—this time at an altitude of about 200 to 300 ft above ground level and with airport operations personnel positioned along the runway to get a better view of the airplane. The second low approach determined that the left MLG was retracted.
The captain stated that, once the fuel was at an appropriate point to execute the gear-up approach and landing, air traffic control vectored the airplane for an ILS approach to the longest runway at the airport. The captain also stated the airplane made a “normal landing touchdown” and that, after the left engine contacted the runway, he maintained directional control with the ailerons, rudder, and right wheel braking. After the captain manually deployed the speedbrakes, the airplane came to a stop on the runway centerline about 2,000 to 3,000 ft from the end of the runway.
A brake rod, which is installed between each brake assembly housing and the shock strut, transfers the torque generated by the brake to the MLG. Each brake rod is connected to the torque arm on the brake assembly housing using, among other things, a pin that is secured by a retaining bolt. Postaccident examination of the left MLG assembly revealed that the No. 6 brake rod (corresponding to the aft inboard wheel) was connected at the shock strut end but was not connected to the torque arm on the brake assembly housing. The brake rod pin was likely in place during the accident flight takeoff given that no scrape marks or gouging were found on the brake rod, indicating that the brake rod had not contacted the runway while the airplane was moving, which would likely have happened if the brake rod was connected only at the shock strut end while the left MLG was in its extended position. The flight crew was unable to extend the left MLG during the approach because the pin had come loose during the flight, which allowed the brake rod to move out of its normal position and become hung up on the landing gear upstop.
The airplane had accumulated 73 flight cycles since the last No. 6 brake assembly change, which would have been the last time that the No. 6 brake rod was removed and reinstalled. The maintenance personnel who performed the No. 6 brake assembly change did not recall anything unusual or concerning about the installation of the brake assembly or brake rod.
The No. 6 brake rod attaching hardware components from the accident airplane were not located after the accident, precluding a determination of why the pin was in place for the takeoff but not when the crew tried to lower the landing gear. As a result, on the basis of the available evidence for this accident, the investigation was unable to determine the reason that the brake rod pin came loose during the accident flight.
Related NOTAM:
!LAX 08/120 LAX RWY 07L/25R CLSD 2008191200-2008192359